Back in late 2022, I spent a lot of time hunting for an electrical gremlin that caused every locomotive crossing the frog at the first swtich coming out of CNR Staging shorting out and stopping. It had me, at my wits end, ready to scream “Trains are StupidTM ” (TM Trevor Marshall). Suffice to say, the problem was not resolved despite my best efforts, and I was nearing the point of doing legitimate damage to the switch trying to file and grind looking for the cause of the short. After a hard day at work this week, I realized that my friend Dan Garcia who built the switches using Fast Tracks jigs, made me two extra turnouts. On my original track plan, everything was a tight Number 4 turnout. He was, convinced that in one location, I had room for a pair of Number 5’s instead, so he built me two ladders of a LH/RH switch in tight sequence. It turned out, he was correct, the Number 5’s did fit, so I used them. This means, somewhere in the house, I have a pair of Number 4 switches, and could potentially “just” rip out the problem switch. That of course, makes it sound like an easier task than it is, but we will get there.


The spare switches located, and the left hand one for the replacement job split from the righthand one.
First up, how to remove the scenery and the existing switch without completely destroying an end of the layout. Fingers crossed, with careful cutting and scraping, I could get it out. Using a variety of knives and edges, I created an edge around the switch I wanted to take out. In some places, my scenery and the ballast crumbled reasonably easy, in others, I used some warm water to try and re-activate the glues to see if the dirt and ballast would soften. These techniques worked, and in a bit of time, I was able to loosen enough ground cover that I could start to see if I could remove the switch. I glued down my track using silicone caulk, So I was hoping I could get a putty knife in and separate it from the pink foam beneath. I was mostly able to do so, not perfectly clean, but clean enough. I wound up having to cut some of the track at either end, while the diverging track the joiners for alignment slid off easily. at the left side of the pictures, the joiners were completely stuck, and I was trying desperately hard to not mess up the alignment with staging.






Starting with partial scenery in place, working on breaking up the scenery, and then fitting in the new switch and cutting the track down to size to fit the gap of the removed switch.
Once I had the track out, I spent some time cleaning up the debris where the track was, and preparing the area for installing a new switch. I then, very carefully started trimming the rails of the new switch to fit. My goal, was for it to drop in, and use rail joiners to ensure the rails stayed aligned. Once it is in and tested, I will paint it in place, then redo the ballast and scenery. For now, the goal is to get the switch in, working, and wired up to test. I was able to drop the switch in so that I didn’t even have to adjust the Fast Tracks Bullfrog control, the throw rod fit into the bar on the new switch, talk about precise trimming and filing! In fact, the new switch is so tightly fit, and sits so smoothly, I am not going to glue it down as I did with the rest of my track. I will allow the ballast and scenery to lock it into place after I work my way through a methodical testing and finishing process. Tonight, I ran all four of my main layout locos and a couple of others through it back and forth and down the diverging track, nothing stalled. Next up, will be painting the ties and track. After that, another round of testing, then if all is OK, on to new ballast. Then more testing. and so on until the scenery is restored to where it was before I started cutting it away.


Ugly looking prior to painting and re-ballasting/re-scenicing, but, locomotives run through it both ways, no stalls, no strange behaviour.
Far and away my most “temperamental” locomotive is my Rapido SW1200RS. Even with a keep alive installed and active, it is a finicky locomotive, and likes to stall. For a long time, I thought it was this locomotive that was the problem, not the switch frog. While I still don’t know what in the frog was shorting out, I reached the point of determining that it was the path of least resistance to just remove the apparently faulty track, and install a new piece of track. The video below shows the Rapido SW1200RS going through the switch in all directions, which trips the Frog Juicer to change polarity, and keep on going. This is something that would not have happened before the swap out.
I am, to put it mildly, incredibly pleased with myself and feel quite clever. Between the realization I had all the tools I needed to swap a switch, and having the new switch seemingly work, really makes me feel good about the layout. To be honest, I hadn’t done a lot of layout work the past few weeks, but being able to run trains and feel they may work could get me back in the groove here for April and into the summer!